Timeline
03/16/09:
- 15:42 team edited by
- Added team photo (it's probably a bit large...) (diff)
- 13:44 membership edited by
- (diff)
03/15/09:
- 20:20 Ticket #49 (Complete Kalman filter shell) closed by
- fixed
- 16:52 Changeset [464] by
- 16:41 Changeset [463] by
- fixed DRC errors (clearance, width) for 16 mil clearance
- 15:57 Changeset [462] by
- header updates
- 01:43 Changeset [461] by
- License fixes; hopefully fixed motor speed graphing for real motors
03/14/09:
- 17:59 Changeset [460] by
- Inverted the speed graph
- 17:41 Changeset [459] by
- Added shell to GUI
- 16:57 Changeset [458] by
- Fixed graph issues
- 16:54 Changeset [457] by
- more cleanup
- 16:31 Changeset [456] by
- updated the mcc board
03/12/09:
03/11/09:
- 21:51 Changeset [455] by
- thresholding in OpenCV
- 21:25 Changeset [454] by
- Changes from the robot; GUI stuff, mainly
- 20:17 Changeset [453] by
- 20:14 Changeset [452] by
- uncommented function
- 20:13 Changeset [451] by
- quicked time to kill robot for new killswitch
- 20:07 Changeset [450] by
- fixed for new killswitch
- 19:03 membership edited by
- (diff)
- 19:01 meetings/2009-03-10 created by
- Posted yesterday's minutes
- 18:53 meetings edited by
- Added links (diff)
03/10/09:
- 20:18 Changeset [449] by
- Added get gain button
03/09/09:
03/08/09:
- 17:35 Changeset [448] by
- …
- 15:51 Changeset [447] by
- added gps
- 14:41 Changeset [446] by
- changed killswitch digital out pins, changed switching.
03/07/09:
- 02:49 Ticket #48 (Data logging) closed by
- fixed: I have tentatively completed this in changeset [420], though it needs …
- 02:48 Changeset [445] by
- Added data logging re #48; added Wiimote control to GUI
03/06/09:
- 15:50 Changeset [444] by
- untested updated code for killremote, ading power led, link led, and …
03/05/09:
- 23:30 Ticket #48 (Data logging) created by
- (23:15:30) chtr: would it be possible for you to get logging of the …
- 23:15 Ticket #43 (Make microstrain software automatically reconnect) closed by
- fixed: I completed this a while ago.
- 20:01 Changeset [443] by
- redid ground bus
- 16:12 Changeset [442] by
- added first draft of killboard board, need to redo power busses
- 15:29 Changeset [441] by
- added schematic for robot killswitch receiver
03/04/09:
- 22:34 Changeset [440] by
- redid the molex board a bit…
- 17:15 Changeset [439] by
- make drc happy
- 17:12 Changeset [438] by
- changed some cap positions
- 03:04 Changeset [437] by
- added draft single layer molex distro board
03/03/09:
- 17:56 Changeset [436] by
- cleaned up the routing a bit
- 17:43 Changeset [435] by
- cleaned up the ground bus a tad
- 17:38 Changeset [434] by
- added ground bus, wired up supply on inverter
03/02/09:
- 22:33 Changeset [433] by
- board files for motor controller, incomplete
02/28/09:
- 15:19 Changeset [432] by
- commit before cleanup
02/25/09:
- 23:53 Changeset [431] by
- Added controller mode stuff
- 23:33 Changeset [430] by
- Completed gain modification GUI
- 21:38 Changeset [429] by
- …
- 20:08 Changeset [428] by
- Added more gain widget callbacks
- 20:04 Changeset [427] by
- Added more gain widgets
- 19:58 Changeset [426] by
- Added gain fields to GUI
- 19:01 Changeset [425] by
- Added crude speed graphing
- 16:16 Changeset [424] by
- Tweaks
- 15:34 igvc/electronics-todo edited by
- (diff)
- 15:34 igvc edited by
- Removed legacy motor controllers (diff)
- 14:20 software/system-overview edited by
- Added some up-to-date documentation (diff)
- 13:33 igvc edited by
- removed software "getting started" page (diff)
- 13:30 igvc edited by
- Updated status messages (diff)
02/21/09:
- 22:24 Changeset [423] by
- added support for status LEDs
02/20/09:
- 19:11 Changeset [422] by
- fixing bugs in the python motor code
- 17:50 Changeset [421] by
- convertin speeds
- 17:44 Changeset [420] by
- adding fancyier drive code, and support for more motor controller commands
- 17:33 Changeset [419] by
- Added locking and recovery to motor controller
- 16:11 Ticket #22 (Find a decent digital compass) closed by
- invalid
- 16:07 Changeset [418] by
02/19/09:
- 22:46 Changeset [417] by
- fixed bug that would cause the robot to lurch if the physical estop button …
- 22:45 Changeset [416] by
- made Rgetspeed return same units used in Tsetspeed, signed RPM
- 21:41 Changeset [415] by
- added descriptions of commands
- 21:33 Changeset [414] by
- restored failsafer code to killswitch
- 21:29 Changeset [413] by
- commenting out debug messages, having shell stop the motors when it's done
- 21:25 Changeset [412] by
- running was set to be false in Controller.init
- 21:23 Changeset [411] by
- re-setting motors to be running (this shouldn't really be needed, but oh …
- 21:15 Changeset [410] by
- 21:05 Changeset [409] by
- adding debugging to _recieve
- 20:44 Changeset [408] by
- sending directly instead of packing in structs
- 20:28 Changeset [407] by
- more debugging
- 20:08 Changeset [406] by
- adding debuggin
- 13:26 Changeset [405] by
- update the mkfiles
02/18/09:
- 22:50 Changeset [404] by
- moving drive speeds to gui.py
- 22:42 Changeset [403] by
- factoring out analog code and deleting digital code
- 22:16 Changeset [402] by
- Fixed compass positioning
02/17/09:
- 23:32 Changeset [401] by
- also new in revision 400, my amazing ability to fail at resolving …
- 23:26 Changeset [400] by
- revision 400! added eeprom writing, gain setting, and speed retrieval
- 20:44 Changeset [399] by
- minor fixes
- 20:40 Changeset [398] by
- Working refactoring the startup stuff
- 19:29 Changeset [397] by
- 19:15 Changeset [396] by
- updated killswitch
- 19:04 Changeset [395] by
- 18:46 Changeset [394] by
- comitted robot kill with 8MHz
- 18:35 Changeset [393] by
- added kill robot hex
- 18:34 Changeset [392] by
- added killremote hex
- 18:29 Changeset [391] by
- added killswitch source
- 17:59 Changeset [390] by
- it's amazing how many stupid mistakes you can make
- 01:31 Changeset [389] by
- added timeout for loss of serial comms
- 00:32 Changeset [388] by
- should be using eeprom to store gains…
02/16/09:
- 20:16 Changeset [387] by
- changed the _send method to work
- 16:34 membership edited by
- (diff)
- 10:39 Changeset [386] by
- improvements
02/15/09:
- 23:19 Changeset [385] by
- fixed the problem with spurious bytes
- 19:40 Changeset [384] by
- that's what i get for not compiling with -Wall…
- 18:46 Changeset [383] by
- motor controllers are mostly working
- 17:06 Changeset [382] by
- Changes
- 17:01 Changeset [381] by
- more settings
- 16:52 Changeset [380] by
- forgot the speed
- 16:51 Changeset [379] by
- changed mkfile
- 16:42 Changeset [378] by
- Motor controller fix
- 16:14 Changeset [377] by
- New motor controller code
- 13:19 Changeset [376] by
- commited pc testing code
- 11:45 Changeset [375] by
- some changes from last night.
02/14/09:
- 17:16 Changeset [374] by
- p works
Note: See TracTimeline
for information about the timeline view.